Go Back   The Ford Barn > General Discussion > Late V8 (1954+)

Sponsored Links (Register now to hide all advertisements)

Reply
 
Thread Tools Display Modes
Old 11-05-2020, 11:57 AM   #81
yblock57
Senior Member
 
yblock57's Avatar
 
Join Date: Oct 2020
Location: Round Rock, TX
Posts: 128
Default Re: Fordomatic late shifting ('57 thunderbird)

Daves55Sedan —

I should've been more clear in my original post. This setup had linkage issues due to the throttle valve being installed wrong in the valve body which limited the movement of the throttle rod. Dad drove the car before we realized what was going on and inadvertently floored the accelerator to get the trans to kick-down. This caused the throttle to become stuck in the wide-open position (or close to wide-open). He had to turn the key off. Luckily no damage to the engine or car, but it bent the threaded end of the throttle rod and unbeknown to us, the 'double-L' piece on the firewall.

Once I ascertained all my pieces were correct for a '57 D model (measured a friend's correct setup), I pulled the 'double-L' piece out of the car and proceeded to carefully bend it in the direction if needed to go. The ease at which it bent left no doubt in my mind that this was the key to all this linkage mess.

Once it went back in, the shop manual procedures were followed and this time everything went exactly as outlined.

Appreciate everyone's input here. I should be putting it all back together sometime next week and will post my results. Fingers crossed!
__________________
Kent — Round Rock, TX

'56 F-100 | '56 Crown Vic | '57 Fairlaine 500 | '57 Thunderbird
yblock57 is offline   Reply With Quote
Old 11-30-2020, 12:07 AM   #82
bbrocksr
Senior Member
 
Join Date: May 2010
Location: Yakima Washington
Posts: 913
Default Re: Fordomatic late shifting ('57 thunderbird)

Quote:
Originally Posted by yblock57 View Post
Daves55Sedan —

I should've been more clear in my original post. This setup had linkage issues due to the throttle valve being installed wrong in the valve body which limited the movement of the throttle rod. Dad drove the car before we realized what was going on and inadvertently floored the accelerator to get the trans to kick-down. This caused the throttle to become stuck in the wide-open position (or close to wide-open). He had to turn the key off. Luckily no damage to the engine or car, but it bent the threaded end of the throttle rod and unbeknown to us, the 'double-L' piece on the firewall.

Once I ascertained all my pieces were correct for a '57 D model (measured a friend's correct setup), I pulled the 'double-L' piece out of the car and proceeded to carefully bend it in the direction if needed to go. The ease at which it bent left no doubt in my mind that this was the key to all this linkage mess.

Once it went back in, the shop manual procedures were followed and this time everything went exactly as outlined.

Appreciate everyone's input here. I should be putting it all back together sometime next week and will post my results. Fingers crossed!
How did it work out?
Bill
bbrocksr is offline   Reply With Quote
Sponsored Links (Register now to hide all advertisements)
Old 11-30-2020, 06:56 PM   #83
yblock57
Senior Member
 
yblock57's Avatar
 
Join Date: Oct 2020
Location: Round Rock, TX
Posts: 128
Default Re: Fordomatic late shifting ('57 thunderbird)

Quote:
Originally Posted by bbrocksr View Post
How did it work out?
Bill

Hey Bill. Thanks for checking in. The valve body was reinstalled and trans closed back up. Was able to get all linkage adjusted correctly per the manual.

Went ahead and pulled the pinion seal to replace as it was leaking badly. Car is still on stands while I wait for parts. Addressing several other things at the same time. Seems like a never ending list!

Will update when I get it back on the ground. Fingers crossed [emoji1695]

Thanks
__________________
Kent — Round Rock, TX

'56 F-100 | '56 Crown Vic | '57 Fairlaine 500 | '57 Thunderbird
yblock57 is offline   Reply With Quote
Old 11-30-2020, 07:27 PM   #84
Gene F
Senior Member
 
Gene F's Avatar
 
Join Date: Mar 2012
Location: Ohio
Posts: 1,951
Default Re: Fordomatic late shifting ('57 thunderbird)

How did the pinion seal project go? How did you do that? Seems like there are two seals. Did you order them both, or how do you know which one you need, and where did you get it?
Gene F is offline   Reply With Quote
Old 11-30-2020, 08:09 PM   #85
yblock57
Senior Member
 
yblock57's Avatar
 
Join Date: Oct 2020
Location: Round Rock, TX
Posts: 128
Default Re: Fordomatic late shifting ('57 thunderbird)

Quote:
Originally Posted by Gene F View Post
How did the pinion seal project go? How did you do that? Seems like there are two seals. Did you order them both, or how do you know which one you need, and where did you get it?

Hey Gene —

I ordered both seals — outer pinion seal and square cut pinion support O-ring. I also ordered a crush sleeve eliminator kit and new pinion nut.

Parts came from multiple places as I tend to shop around for the best deals. Outer pinion seal is an SKF neoprene #18276 that I got from of all places Home Depot for $9.24 shipped! Thunderbird suppliers are asking $86 for that same seal! The pinion support O-ring is a ford part from eBay #B7A-4669-B for $15.95 shipped. The rest of the parts came from bronco graveyard — crush sleeve eliminator kit #22293 $19 & pinion nut #22294 $4.

Hopefully get the stuff next week. Been cleaning up parts in preparation.
__________________
Kent — Round Rock, TX

'56 F-100 | '56 Crown Vic | '57 Fairlaine 500 | '57 Thunderbird
yblock57 is offline   Reply With Quote
Old 12-01-2020, 02:14 AM   #86
KULTULZ
Senior Member
 
KULTULZ's Avatar
 
Join Date: Aug 2012
Location: IN A 'GALAXIE' FAR FAR AWAY
Posts: 6,464
Thumbs up Re: Fordomatic late shifting ('57 thunderbird)

Sponsored Links (Register now to hide all advertisements)
Quote:
Originally Posted by yblock57 View Post

The rest of the parts came from bronco graveyard — crush sleeve eliminator kit #22293 $19 & pinion nut #22294 $4.
Did not know a commercial kit was available. Good choice.
Attached Images
File Type: jpg REAR - Crush Sleeve Eliminator Kit.jpg (23.7 KB, 14 views)
__________________
*****

- WHY IS IT ... -

... that everything you buy in the grocery store is either wrapped in or contained in plastic but the government doesn't want you to carry it out in a plastic bag?

WONDERING IN W(BY GOD)V ...

DIAGNOSED CDO - (OCD In Correct Alphabetical Order)

Last edited by KULTULZ; 12-01-2020 at 02:20 AM.
KULTULZ is offline   Reply With Quote
Old 12-01-2020, 09:01 AM   #87
yblock57
Senior Member
 
yblock57's Avatar
 
Join Date: Oct 2020
Location: Round Rock, TX
Posts: 128
Default Re: Fordomatic late shifting ('57 thunderbird)

Quote:
Originally Posted by KULTULZ View Post
Did not know a commercial kit was available. Good choice.

Thanks. I didn’t know of this kit either. Was pointed to it by a very knowledgeable fellow on the yblocksforever forum [emoji1303]
__________________
Kent — Round Rock, TX

'56 F-100 | '56 Crown Vic | '57 Fairlaine 500 | '57 Thunderbird
yblock57 is offline   Reply With Quote
Old 12-10-2020, 07:44 PM   #88
Gene F
Senior Member
 
Gene F's Avatar
 
Join Date: Mar 2012
Location: Ohio
Posts: 1,951
Default Re: Fordomatic late shifting ('57 thunderbird)

So is this installed now? How did you make out?
Gene F is offline   Reply With Quote
Old 12-10-2020, 10:33 PM   #89
yblock57
Senior Member
 
yblock57's Avatar
 
Join Date: Oct 2020
Location: Round Rock, TX
Posts: 128
Default Re: Fordomatic late shifting ('57 thunderbird)

Quote:
Originally Posted by Gene F View Post
So is this installed now? How did you make out?

Not yet. Hopefully this coming week.
__________________
Kent — Round Rock, TX

'56 F-100 | '56 Crown Vic | '57 Fairlaine 500 | '57 Thunderbird
yblock57 is offline   Reply With Quote
Old 12-17-2020, 05:39 PM   #90
yblock57
Senior Member
 
yblock57's Avatar
 
Join Date: Oct 2020
Location: Round Rock, TX
Posts: 128
Default Re: Fordomatic late shifting ('57 thunderbird)

Update: Success!

Just got back from test driving the 'bird. It's like driving a different car now. Everything behaves like it should. Talk about a relief!

Did the pressure test before taking it off the stands (as several of you mentioned) and had to lengthen the rod several turns to get the pressure up to specs. If you baby it down the street, it'll shift about 19 mph. If you drive lightly down a residential street, about 22-23 mph. All relative on throttle pressure — just like the book says. Feels like it's about where it needs to be.

The accelerator is so much lighter feeling and easier to hold. Before it was fatiguing after a while cruising down the highway (due to binding).

Wanted to thank everyone who answered on this thread and shared their knowledge. It is GREATLY appreciated. Everything I've learned during this fiasco is going in the vault and should hopefully help me or someone else in the future. This is a great site and the level of knowledge and helpfulness is very humbling. Thanks again for helping get this old 'bird back on the road!
Attached Images
File Type: jpg 57bird.jpg (105.5 KB, 16 views)
__________________
Kent — Round Rock, TX

'56 F-100 | '56 Crown Vic | '57 Fairlaine 500 | '57 Thunderbird
yblock57 is offline   Reply With Quote
Old 12-17-2020, 05:45 PM   #91
scicala
Senior Member
 
scicala's Avatar
 
Join Date: Jun 2010
Location: Detroit suburb, MI
Posts: 3,698
Default Re: Fordomatic late shifting ('57 thunderbird)

I'm glad you got it all figured out and fixed. Enjoy the car.
Also, thanks for posting the final results.

Sal
scicala is offline   Reply With Quote
Old 12-18-2020, 05:37 PM   #92
Gene F
Senior Member
 
Gene F's Avatar
 
Join Date: Mar 2012
Location: Ohio
Posts: 1,951
Default Re: Fordomatic late shifting ('57 thunderbird)

Glad it's fixed. That TV rod length is a fussy thing.
Gene F is offline   Reply With Quote
Old 12-18-2020, 05:41 PM   #93
yblock57
Senior Member
 
yblock57's Avatar
 
Join Date: Oct 2020
Location: Round Rock, TX
Posts: 128
Default Re: Fordomatic late shifting ('57 thunderbird)

Quote:
Originally Posted by Gene F View Post
Glad it's fixed. That TV rod length is a fussy thing.
It sure is. Never realized until things went haywire. Glad it ended up being fixable in the car instead of having to pull everything back out again!

Quote:
Originally Posted by scicala View Post
I'm glad you got it all figured out and fixed. Enjoy the car.
Also, thanks for posting the final results.

Sal
Appreciate it! Didn't want to leave the thread unresolved. Maybe this can help someone else out someday.
__________________
Kent — Round Rock, TX

'56 F-100 | '56 Crown Vic | '57 Fairlaine 500 | '57 Thunderbird
yblock57 is offline   Reply With Quote
Reply

Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump

Sponsored Links (Register now to hide all advertisements)


All times are GMT -5. The time now is 08:35 AM.