Re: Decided to pull the motor/trans
Update. Motor and trans are back together and in the car. The motor got new pistons and rings, {.0125 over), cylinders honed to .004 piston/wall clearance, checked bearing clearances, all but one were between -0015 and .002, the other was about .0025 so I removed one shim, replaced head studs and replaced the ring gear. Trans was disassembled and inspected, replaced both shafts and rebuilt the shifter ball. Trans case and tower powder coated black as well as the clam shell halves. Motor and bell housing painted ford green. Have put on about 180 miles, runs great and no sign of oil use. far cry from the 1qt per 60 miles before.
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