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Old 03-11-2012, 12:30 PM   #23
flthd31
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Join Date: May 2010
Location: Northwest PA
Posts: 25
Default Re: Fired my flathead today for the first time!!!

Quote:
Originally Posted by Chris View Post
You had a leaky head and had water some into the combustion chamber? You ran a dial indicator on it and the piston came up to the same specs as the others? I don't see how a rod can bend and still be the same height. Did you check yours for plat up and down, side to side? We did on mine, it was nice and tight up and down, and had slight play side to side like it should. I'm not arguing, just trying to understand what happened in your engine.
The car was a 47 coupe with a 49 Merc that was just rebuild. It was bored .125 over, Isky Max1 cam. Entire reciprocating assy was balanced with flywheel and pressure plate. Ran smooth as silk and tacked up to 5000 very quickly. 2 97's on Elelbrock intake and Edelbrock heads. It had about 500 miles on it.
Back then, big bore head gaskets were impossible to find and I was using some graphite composites that turned out to be junk. The water seeped in after sitting for a few days. When I started it on a Sat morning, I had the exact experience you had with water flowing out of the header. I pulled the head and could see where the gasket failed.
The head was fine with no damage. I have a set of hydro test plates (head and water pump), so we put them on to make sure the block wasn't cracked...tested ok.
Next we checked the rise of the piston with a dial indicator and it looked good. In hind sight, we think the rod may have been twisted slightly.
All I can say is that those old Fords rods are tough, but they can't compress water...something has to give. Maybe that's what cracked your head?
If i could go back in time, I would have torn it down, not that big of a deal compared to a total loss of a new engine.

Last edited by flthd31; 03-11-2012 at 03:38 PM.
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